The smooth part of the shaft wasn't long enough which left the drive pulley sitting on threads. This didn't seem sensible to me. I determined the shaft's proper length and cut the excess off. That was a good start but it left the threads under the drive pulley. I removed them by turning the last inch or so of the shaft down to 1/2" from 3/4". Then I made a sleeve that would bring the diameter back up to 3/4" by boring a 1/2 hole in an aluminum rod. I pressed this to the shaft. It was a tight one-way fit. Finally, I turned the sleeve to the proper diameter, faced the end of the shaft, and broke the corners.
This was the first press fit of this size that Marco and I had ever done. It could be likened to monkeys doing math.
If I'd had the steel, I would have made the sleeve from that. We'll see how long the aluminum lasts.
Here are pictures of the countershaft in place.
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While I had it all apart, I decided I didn't like the retaining collar on the right end of the countershaft and the pulley on the left end rubbing against the casting. Didn't seem too make a lot of sense. As an experiment I cut some washers from a plastic jug. We'll see how long they last. I don't expect they'll have too much pressure on them.